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NASA Technical Memorandum 107309 AIAA-96--2622

Metallized Gelled Propellants: Oxygen/RP-1/ Aluminum Heat Transfer and Combustion Measurements

Bryan Palaszewski Lewis Research Center Cleveland, Ohio and

James S. Zakany NYMA, Inc. Brook Park, Ohio

Prepared for the 32nd Joint Conference cosponsored by AIAA, ASME, SAE, and ASEE Lake Buena Vista, Florida, July 1-3, 1996

National Aeronauticsand Space Administration

METALLIZED GELLED PROPELLANTS: OXYGEN/RP-1/ALUMINUM ROCKET HEAT TRANSFER AND COMBUSTION MEASUREMENTS

Bryan Palaszewski* NASA Lewis Research Center Cleveland, OH 44135

James S. Zakany NYMA, Inc. Lewis Research Center Group Brook Park, OH 44142

Abstract metallized gelled RP-1/A1 show that the peak nozzle heat fluxes with the metallized A series of heat transfer gelled 02/RP-1/A1 propellants are substantially experiments using metallized gelled higher than the baseline 02/RP-l: up to double propellants was conducted. These experiments the flux for the 55-wt% RP-1/A1 over the RP-1 used a small 20- to 40-1bf thrust engine . Analyses showed that the heat composed of a modular injector, igniter, transfer to the wall was significantly different chamber and nozzle. The fuels used were for the RP-1/A1 at 55-wt% versus the RP-1 traditional liquid RP-1 and gelled RP-1 with fuel. Also, a gellant and an aluminum 0-, 5-, and 55-wt% loadings of aluminum combustion delay was inferred in the 0% and 5- particles. Gaseous oxygen was used as the wt% RP-1/A1 cases from the decrease in heat oxidizer. Three different injectors were used flux in the first part of the chamber. A large during the testing: one for the baseline O2/RP- decrease in heat flux in the last half of the 1 tests and two for the gelled and metallized chamber was caused by fuel deposition in the chamber and nozzle. The engine combustion gelled fuel firings. Heat transfer measurements were made with a rocket engine calorimeter occurred well downstream of the injector face chamber and nozzle with a total of 31 cooling based on the heat flux estimates from the channels. Each channel used a water flow to temperature measurements. carry heat away from the chamber and the Nomenclature attached thermocouples and flow meters allowed heat flux estimates at each of the 31 stations. The rocket engine Cstar efficiency AI Aluminum for the RP-1 fuel was in the 65-69% range, Cstar Characteristic velocity (m/s) while the gelled 0-wt% RP-1 and the 5-wt% OF Fahrenheit degrees RP-1 exhibited a Cstar efficiency range of 60 to I_p 0bf-s/lbm) 62% and 65 to 67%, respectively. The 55- IRFNA Inhibited Red Fuming Nitric wt% RP-1 fuel delivered a 42-47% Cstar Acid efficiency. Comparisons of the heat flux and K Kelvin temperature profiles of the RP-I and the MMH Monomethyl 02 Oxygen

* AIAA Senior Member, Program Manager, Fuels and Space Propellants for Reusable Launch - Small Business Innovation Research (SBIR) Focused Topic lbf pound-force scale engine, but the data would nonetheless Q/A Heat flux fMW/m2) help guide future large-scale testing efforts. RP-1 -1 These experiments were also done to identify conditions or metal loadings that will provide T Temperature (K or OF) better efficiency and other information that will wt% Weight Percent of Fuel Mass improve the thinking in future trade studies.

l gmma Experimental rocket engine heat transfer and combustion measurements were conducted Metallized gelled liquid fuels have the potential for increasing the specific impulse, the with metallized gelled O2/RP-1/AI. Three density, and the safety of rocket propulsion different gelled fuels were used including 0-, 5-, and 55-wt% RP-1/A1. Traditional RP-1 systems.t-16 While the benefits and military was used as the basis of comparison. A water- applications of Earth-storable (IRFNA/MMH) cooled calorimeter chamber and nozzle were gelled and metallized gelled fuels and oxidizers used to measure the heat flows in the rocket are well established, some questions still exist engine. Traditional 4- and 8-element triplet regarding their application for NASA missions. injectors with oxidizer on the outer flow paths Oxygen/RP-1/A1 and cryogenic metaUized (O-F-O) were used. Three injectors were used: gelled propellants show promise in the design two were designed for metallized gelled studies for NASA missions, assuming an propellants and one for the traditional RP-1. engine efficiency comparable to traditional The calorimeter engine hardware and injector liquid fuels. In the mission studies, there was designs were derived from NASA Lewis' past a relatively limited range of efficiency where programs. These tests were planned to metallized propellants were most effective in determine the potential metal combustion lag reducing booster size and improving delivered caused by aluminum combustion in the multi- payload. Experimental efforts to resolve the phase flow typical of metallized gelled performance issue were therefore planned and propellants. They were also planned as a conducted. The questions that arose prior to follow-on to the previously conducted heat sink and during these investigations include: can rocket engine testing to provide data that would propellants be fh-ed successfully in a rocket improve future test engine designs and test engine, what is the combustion efficiency, are programs with metal and gellant combustion in the metallized gelled propellants easily rocket propellants. controlled, and are their flow properties predictable? The NASA experimental work15, After the initial heat sink engine tests, 16 was applicable to small 20- to 40-1bf rocket added testing was conducted with a calorimeter engines and was a fh'st step toward answering chamber and nozzle to find any effects of these questions. While all of the mentioned propellant combustion delay due to the multi- issues have not been fully addressed for all phase fluid in the chamber with the metal thrust levels, the data from these tests can guide particles. As with the heat sink tests, the other future research and help pave the way for purpose of the experiments was to determine successful future testing. the realistic combustion efficiency one might expect for O2/RP-1/A1 metallized gelled fuels This work was conducted in and to see if a rocket combustor could deliver conjunction with the heat sink engine testing the relatively high efficiency needed for discussed in References 15 and 16. The heat successful NASA applications of metallized sink testing showed that a rocket engine can be gelled combustion. Facility limits restricted the fu'ed successfully, that the propellant flow is testing to a small combustor, so the efficiency controllable and that the flow properties are might not be as high as predicted for a full- predictable. Rocket engine performance was anissue,due to the small size of the engine and Boosters (SRB)7, 11.15, the propellant density the relatively large purge flow rates needed to increase allows for shorter boosters. make the engine firing repeatable. Questions Alternatively, for the same booster size, O2/RP- also arose in terms of the propellant exposure l/A1 has the potential for higher payload to air and drying in the feed system and delivery mass over traditional propellants. injector. Many issues were resolved in the With O2/RP-1/AI, the specific impulse is lower heat sink testing, but solutions to the igniter than that for O2/RP-1 propellants, even for the purge effects were not able to be implemented highest payload benefit cases. This payload in the past test program. benefit is enabled because the high density of the gelled metallized fuel allows a larger mass Why Metallized Gelled of propellant to be placed in a smaller volume Propellants? than traditional liquid propellants. Gelled propellants' thixotropic nature also increases Metallized gelled propellants have been safety by minimizing the potential for tank studied analytically and experimentally for over leakage and reduces the spill area in case of an 60 yearst. The historical work has focused on accidental propellant release. the benefits of high specific impulse, high density, and safety2. 3, 4, 5, 6. Current non- Based on rocket engine and NASA uses for these propellants may lie in performance studies, 0,- 5-, and 55-wt% tactical and strategic missiles and aircraft aluminum loadings in RP-1 seemed the most ejection seats3, 4.5, 6. Extensive work has been attractive11. During the course of these conducted with metallized-gelled Earth-storable investigations, it became clear that gelled fuels propellants, such as hydrazine (N2H4), may be more attractive to users than those with Inhibited Red Fuming Nitric Acid (IRFNA), metal particles. A stepping-stone approach and monomethyl hydrazine (MMH).4, 5, 6 where gelled fuels are first used and then the However, these propellants are not planned for users evolve toward metallized gelled use in future NASA launch vehicles. To propellants is a definite option. Future vehicles explore the potential of metallized-gelled fuels, using gelled fuels may allow for slosh NASA chose to pursue the propellant reduction, added safety, and leakage reduction combinations that were more suitable to its Therefore, gelled RP-1 (0 wt%) was one of the selected candidates. The 0-wt% loading future plans in the Metallized Propellant Program7-16. This program, at the NASA provided a basis of comparison to estimate the Lewis Research Center, has been conducting gains or losses of gelling the RP-1. Based on a experimental, analytical, and mission studies parametric engine performance analysis, the 5- since 1987. This program has concentrated on wt% loading delivered the maximum predicted O2/RP-1 and O2/H2 propellant combinations Isp for the Oz/RP-1/AI combinations. This and the issues related to using these gelled was one reason for the selection of this metal propellants with metal particle additives. loading. Another reason is that, based on design of experiments methodologies, the selection of three different metal loadings A series of propulsion and vehicle trades studies7, it, 12, 13, 14 had shown a would show the relative trends in performance, and allow the data to be compared to the potential benefit for metallized gelled fuels for NASA launch vehicles and have indicated that theoretical trends. O2/RP-1/A1 can have significant benefits by Ex_riment Obiectives increasing propellant density. Figure 1, which is derived from data in Reference 11, depicts Rocket performance and heat transfer the potential increases in payload enabled by measurements were desired in this test high-density 55-wt% RP-1/AI. Using O2/RP- program. Since no data were previously l/Al propellants in a Liquid Rocket Booster available for O2/RP-1/AI rocket combustion replacement of the Space Shuttle Solid Rocket heat transfer, rocket calorimeter measurements gellant fraction was 3.5 wt%. When mixing, it were sought and obtained. Testing was is important to add the "dry" elements fast: thereforeconducted with O2/RP-IIAI adding metal, then gellant, then fuel. A very propellantsusing gelledRP-1 with aluminum small wt% of liquid surfactant, Tween 85, was particles.During thecombustion of metal also added as the last component to the 55-wt% particles,the multi-phaseflow createsa metal loaded fuel. The surfactant aids the distributionof liquid,solidand in the formation of the gel network when using a high combustion chamber. There isthereforea metal loading The dry components are also mismatch in thecombustion time scaleof the very powdery, requiring respirator use. gas,theliquidor gelleddropletsand thesolid particles.The heat transfermeasurements were The gelled metallized propellant density envisionedso thatsome estimatemight be is computed using: made of themetal combustion lagforthe aluminum. Both baselinenon-metallized Gel Density (kg/m3) = propellantsand variousmetal loadingswith gelledRP-I were used to compare the combustion temperatureheat fluxprofilesof the differentcombustion environments. The (I- ML) + ML + SIO_ resultsof therelatedheatsink engine testingare RP-I Density AI Density SiO2 Density summarized in References 15 and 16 and the rocketheattransferprofilesas well as their associatedcombustion performance in the where: rocketengine arepresentedin thispaper. ML weight fraction of metal (A1) in the total weight of fuel SIO2 Experimental Setup: Fuels Loading weight fraction of gellant i_n(l Rocket Engine (SiO2) in the total weight of fuel

Fgel Preparation The surfactant is only 0.7% of the mass of the Several types of metallized gelled fuels metallized gelled fuel, so it was not included in with different metal loadings were investigated. the above equation. Based on rocket engine and vehicle performance studies, 0,- 5-, and 55-wt% One-half gallon batches of the fuel were aluminum loadings in RP-1 seemed the most prepared in storage cans. A paint rejuvenator attractive. The 0-wt% loading provided a (or shaker) was used to mix the fuel basis of comparison to estimate the gains or components. The fuel mixing can was losses of gelling the RP- 1 and the 5-wt% typically half filled to allow for more effective loading delivered the maximum theoretical Iq, mixing of the components during the shaking for the O2/RP-1/A1 combinations. process.

All of the propellant mixing was To place the gelled fuel into the piston- conducted in Cell 14 of the NASA Lewis cylinder tank, a transfer tank system was Rocket Laboratories. Table I provides the constructed and consisted of a 10 gallon constituents of the different fuels. The gelled vessel that was rated for 150 psig. RP-1 was prepared with a 6.5-wt% gellant The gelled fuel was poured into the transfer concentration. This gellant wt% was selected tank, and after sealing the tank, it was based on a series of gelling experiments in pressurized to about 70 psig with . which a range of 1-10 wt% gellant was used. Nitrogen was used because gelled fuels will With the 5 wt% RP-1/A1 fuel, 5 wt% gellant dry when exposed to air. Much effort was was added and with the 55 wt% RP-1/AI, the

4 exercisedto minimizethefuel'sair exposure trailers. Nitrogen is used as a purge g.as to priorto actualrockettesting. protect the igniter and engine after engine shutdown. The liquid RP-1 propellant is Combustion Testing Description delivered to the engine using an 8-gallon pressurized tank attached to the cell. Gelled All of the combustion experiments were propellants are pressurized and fed using a conducted in Cell 21 of NASA Lewis Rocket piston-cylinder tank. Mass flow rates of the Laboratories which is configured to test low propellants were measured by Coriolis-type thrust rocket engines (nominally 50 pounds of mass flow meters, in the case of RP-1 and the thrus0 at sea level or altitude conditions. Only gelled propellants, and by pressure transducer minor modifications to the cell were necessary outputs coupled with choked jeweled orifices in to safely handle the gelled RP-1/A1 propellant the feed lines in the case of gaseous mixtures and to capture the exhaust products propellants. Flow of the liquid RP- 1 propellant for analysis and disposal. A propellant feed was limited by cavitating venturis. In all cases, subsystem was installed in Cell 21 to supply upstream load have a direct bearing the engine with gelled metallized propellant. on the mass flow rates of the propellant. The The main component of this system was a high test matrix conditions were satisfied by varying pressure hydraulic piston-cylinder. This piston- these load pressures and by changing the flow cylinder was fed with the propellant mixture control devices. from a pressurized transfer tank. A schematic of the charging system is shown in Figure 2. Several data acquisition systems were The piston cylinder was pressurized with employed to provide the cell operator and the hydraulic fluid. Propellant flow was regulated researcher with timely and complete data. High by limiting the flow of hydraulic fluid into the fidelity research data was collected with a high piston-cylinder. This was accomplished by speed (TRADAR 2.5) computer system. The controlling the fluid pressure upstream of a high speed data acquisition system is used for cavitating venturi. The results of this method highly transient rocket eng.ine measurements of were that the propellant remained fluid and its chamber pressure and engine propellant mass flow rate was held very constant. manifold pressures and TRADAR provides a Variations in the fuel mass flow rate under 50 kHz sampling rate with 100 data channels. different engine conditions were manageable. Immediate performance data was available on Throughout most of the test matrix, the fuel the strip-chart data logging chart recorder. This feed system parameters were kept constant and recorder could display up to 16 channels of the oxidizer load pressures were changed to data sampled at 200 kHz. Steady state data was achieve various propellant mixture ratios. collected and presented by the low speed Another modification to the test cell was the (ESCORT) system, with a 1 second sampling addition of an exhaust recovery system. This rate. The low speed system was used to record modular system of scrubbers, pumps, and more steady state data on propellant line and collection filters allowed the expertment to be tank pressures and temperatures. This system accomplished with far less environmental supports over 100 channels. In addition to impact than any similar test before it in this digital data, each run was recorded by a video facility. Since the exhaust products were camera and saved on video tape. Selected runs collected, they could easily be examined for were also filmed with a high speed film camera further data concerning the combustion of the at 2000 frames per second. Several still fuel mixtures. photographs were taken between and during each run. Extensive photographic records were Except for the RP-1 and RP-I/AI, all of collected of the test hardware before and after the propellants in the cell are provided in run sets. gaseous form. The are 02, H2, and N2. Both the 02 and H2 are used for the engine igniter and are provided from high-pressure Eneine Hardware water feed lines, thermocouples, and flow meters needed in the 31 channels for the heat Rocket engine calorimeter chamber and transfer measurements is high and great care is nozzle experiments were conducted. The needed to assure the data reflect the proper heat calorimeter combustion chamber had a 2.6-inch transfer locations. Approximately one month inside diameter, was 5.875 inches long, and was required for one technician to setup the the calorimeter nozzle had a 0.6-inch diameter calorimeter engine and its measurement throat. The maximum expansion ratio of the devices. nozzle was 4.77:1, though for consistency with the heat sink calculations and measurements, The injectors use an oxidizer manifold the expansion ratio used in the analysis was within the injector body and have a fuel dome 2.4:1. Figure 3 shows a simple diagram of the set atop it. The injector elements used an engine configuration. In conducting these O-F-O triplet design and both four- and eight- tests, hardware was desired to be modular so element patterns were tested. The elements that many injector options could be tested. were arranged to be mutually perpendicular. Also, any damaged hardware could be removed Due to the use of a gelled metallized fuel, there and easily replaced. is the potential of the RP-1 evaporating and the remaining mix of particles and gellant drying in A total of 22 cooling channels were the fuel passages. Using a removable fuel built into the calorimeter chamber and the dome minimized the potential of propellant calorimeter nozzle had 9 cooling circuits. Table particles being trapped in a complex set of flow II provides the locations of each station in the passages in the internal body manifold. During chamber and nozzle. Numerous thermocouples the testing, a wide range of oxidizer-fuel ratios are located in the cooling passages of the (O/F) were investigated. The injectors were calorimeter combustion chamber. Two designed for an O/F range of 1.2-4.2 for thermocouples were used per cooling circuit. O2/RP-1 and 1.4-3.7 for O2/RP-1/A1. Multiple thermoeouples were desired to find any changes in the chamber temperature The igniter assembly consisted of a perimeter. Temperature measurements were 3.437 cm 3 (0.210 in 3) volume hydrogen- also made for the water entering and exiting the oxygen mixing chamber, a spark igniter, and a cooling channels. These measurements were 0.475 cm (0.187 in) diameter flame the primary method of estimating the heat flux propagation tube. Hydrogen and oxygen in each channel. Standard heat transfer entered the mixing chamber through opposing calculations are performed with this data to inlets. Hydrogen was also directed along the estimate the heat flux at each station. 172° exterior of the flame propagation tube to cool it. During operation, the engine uses a water flow A high O/F ratio was maintained in the igniter of 0.1-1.0 gallons per minute in each of 31 assembly to reduce the flame temperature. The flow channels. The flow meters were of a excess hydrogen ported along the exterior of turbine type and a venturi type (using a the flame propagation tube reduced the local pressure difference (AP) transducer) and were O/F ratio near the injector face, resulting in a used to measure the water flow rates. The much hotter ignition flame. turbine flow meters measured the water flow rates in the cooling channels and with the Engine Mounting. Start Up. thermocouple data on the inlet and outlet and_Stmldmm temperature of each channel, the heat flux was calculated. The heat transfer results from the The engine, including the injector, channels with the turbine flow meters were igniter, chamber and nozzle, was mounted to compared to the heat fluxes computed with the the test stand with stainless steel rods that are adjacent venturi flow meters' measurements screwed into and protrude from the injector (with the AP transducers). The number of the body. All of the engine components were

6 assembledwith threadedbolts. Threemetal Also during the testing, there tended to sealsandone elastomeric O-ring are needed for be a small buildup of gelled fuel in the assembling and sealing the engine components. converging region and this buildup was, in After the engine is mounted in the test stand, part, from the small amount of fuel that flowed the major connections are for the primary fuel from the injector after engine had shut down. and oxidizer manifolds, the igniter fuel and The residual pressure in the fuel mainfold forces this small amount into the chamber. oxidizer and the purge flows for all of the flow paths except the primary fuel. A typical With the engine mounted horizontally, this buildup of propellant was located primari!y on ignition sequence begins with the O2/H2 torch igniter f'wing for 1 second, and after 0.2 to 0.4 the lower portion of the nozzle's converging section and the buildup reached a maximum seconds of operation, the fuel and oxidizer are amount in the nozzle. This buildup had several turned on, with a 0.2 to 0.3 second fuel lead. noticeable effects on the combustion. When After main engine ignition has fwing the gelled fuel with 0- and 5-wt% RP- l/A1, the bottom of the exhaust plume tended to occurred, the igniter flow is shut off and a nitrogen purge is initiated to prevent the igniter appear clear, while the upper portion was much from being consumed by the main combustion more optically thick or white. This propellant flow. This purge flow pressure is a minimum buildup seemed to sweep particles out of the of 30 psi higher than the main chamber lower part of the plume. The effects of this pressure to assure that no combustion products sweeping may be the cause of the somewhat larger dispersions in the I_p efficiencies of the 0- build up in the thin igniter tube. The purge flow significantly increased the total flow rate and 5-wt% RP-l/Al tests when compared with such that the Nz mass flow rate was anywhere the ungelled RP-1 and 55-wt% RP-1/Ai. from 40-70 percent of the total engine flow Heat Transfer and Combustion Experiments: rate. Figure 4 shows the effect of the added Results, Discussion, and Qbservations nitrogen flow on the chamber mixture ratio. The O/F is plotted versus the chamber mixture ratio (O/Fc), where the O/Fc is computed Engine Performance and Efficiency assuming that the nitrogen flows are "fuels" The results presented here are based on and this mass flow is in the denominator or" initial analyses of the test data. All of the results presented here are for the heat sink O/Fc = Oxidizer flow rate engine. The overall Isp, Cstar efficiency, Isp Fuel flow rate + N2 purge flow rate efficiency, and other important data are presented to show some of the important features and potential difficulties with In the figure, it is clear that the O/F can metallized gelled fuels. The theoretical engine be seriously affected by the nitrogen purge flow. All of the cases, regardless of O/F, are performance Is was calculated using a standard strongly influenced. These purge flow rates rocket performance computer code for each fuel were included in all of the Isp calculations, and type and it is used to estimate the Isp and Cstar the added nitrogen does significantly reduce the efficiencies. overall engine Isp. Table llI shows a typical case for the 55-wt% RP-1/Ai. The total N2 The simplified computations for Isp, Cstar flow in the engine caused the overall O/F to be efficiency and Isp efficiency are shown below: 0.24, whereas the main combustion flow had an O/F of 2.00. Though the high N2 flow was Ex_rimental Vacuum Specific not the only contributing factor, the overall result was Cstar efficiency for the engine of only 47%. IVT = F 0bf.-s/lbm) WTOT

7 where: where: IVT = Experimental Vacuum Specific Impulse Q heat flux for segment n F = Thrust level (MW/m 2) WTOT = Total Mass Flow Rate in the Engine WCOOL coolant flow rate per segment (including N2 purges) Ocg/s) Cp Specific heat of water F=CF* Pc* MPL *AT Dr temperature rise for segment n (temperature in K) where: ARC(K)L surface area c.42oled by CF = Thrust coefficient at nozzle exit (using segment n (m) Ref. 22) Pc = Chamber Pressure MPL = Momentum Pressure Loss AT = Throat area The preliminary, test results of Isp, Cstar efficiency and Isp efficiency are plotted versus the main combugtor O/F range tested for each fuel and these figures are described in the CSXP= Pc* MPL* AT* G (ft/s) succeeding sections. The O/F provided in the WTOT figures is the main combustor O/F, and not where: the chamber O/F (O/Fc) described in a CSXP = Experimental Cstar preceding section. In each set of data for the G = Gravitational Constant gelled fuels, there is a wider range of variability than that seen with the ungelled RP-1. This NCSP. C-star efficiency (based on variability is caused by the deposits of metal in chamber pressure) the chamber and the nozzle, the erosion of the injector, and the potential of gelled propellant NCSP = CSXP * 100 (%) density variations as the propellant flowed CST through the feed system to the injector. This where: introduced some uncertainty in the mass flow CST = Cstar predicted using Ref. 15 rate, but these were small after gaining experience with the feed system. These effects are described in the section on observations. /_ efficiency. Figures 5, 6, and 7 summarize the NISPP = IVT * 100 (%) results. In Figure 5, the maximum Isp IVAC produced by each fuel and the range of I_p where: variation near the maximum value are shown. NISPP = Isp efficiency The theoretical predictions, which included the IVAC = theoretical vacuum specific impulse nitrogen purge flow, do not precisely match predicted using Ref. 22. the experimental trends for the 0- and 5-wt% RP-1/AI. The trend is not concerning the Heat Transfer Calculations values of the Isp, but the relation between the different values. With the 0- and 5-wt% RP- The simplified heat transfer I/AI, the theoretical trend is a small increase in computations are described below (Ref. 17- Isp for both of these fuels over RP-1 and a 20). The average heat flux per segment is: reduction in Is 1,for the 55-wt% RP-1/AL While a small increase in Isp was predicted for Qn = WCOOL * Cp * DT a the 0- and the 5-wt% RP-IlA1, there was no ARCOOL increase in Isp for the 0-wt% RP- l/A1 over RP- 1 that is demonstrated in the experimental data. engine's Cstar efficiency which was a There is, however, a very small increase in the maximum of 62% at an O/F of 2.6. The experimental Isp going from the 0-wt% RP- maximum Isp efficiency for the 0-wt% RP-1 l/Al to the 5-wt% loading, consistent with the was 53% and the data for the range of O/F predicted theoretical trend. The 55-wt% RP- ratios are shown in Figure 13. l/Al follows the reduced Isp trend noted in the RP-1/AI: 5-wt% A1. theoretical predictions.

Figure 6 shows the Cstar efficiency As shown in Figure 14, at a 5 wt% RP- ranges (near the maximum I_p values) from the l/A1 loading, the maximum Isi, occurred at an O/F of 2.0 and was 127.1 lbrddlbm and the experiments. All of the fuels showed a low upper bound on the Cstar efficiency: from 47 lowest Isp at this O/F was 97.3 lbrs/lbm. Also, percent (55-wt%) to 69 percent (RP-1). The the performance has a band of variability at the RP-1 varied from 65 to 69 percent and the maximum of the O/F range, but the variation is gelled RP-1 (0 wt%) had a range of 60 to 62 narrow and the performance was more percent. The 0-wt% RP-l/Al showed the repeatable compared to the 0-wt% and smallest variation in the efficiency. With the 5- 55-wt% RP-l/Al. Using 5-wt% O2/RP-l/A1, a wt% fuel, the dispersion in efficiency was from range of 65 to 67% Cstar efficiency was 65 to 67 percent, while the 55 wt% variability delivered. The efficiency data, provided in was 42 to 47 percent. A summary of the Isp Figure 15, was relatively constant over the efficiency is presented in Figure 7 and all of the range. The Isr efficiency, depicted in Figure gelled fuels had similar variations in the 16, had a maximum of 58% at an O/F of 1.3. efficiency data. The RP-1 efficiency only RP-1/AI: 55-wt% Al. varied from 55-61 percent, while the gelled RP- 1 (0 wt%) efficiency ranged from 52-53 percent. The other fuels had a slightly As shown in Figure 17, at a 55 wt% broader range of variation, with 52 to 58 RP-1/AI loading, the I6p peak occurred in the percent with the 5-wt% RP-1/A1 and 36 to 40 range of an O/F of 2.0. The peak Isp was 79.7 percent with the 55-wt% fuel. lbf-s/lbm at an O/F of 2.0. Also, the performance varied over a relatively narrow range over the entire range of O/F. Figures 18 and 19 show the Cstar efficiency and Isp Figure 8 presents the Is.pversus O/F for efficiency versus O/F for 55-wt% gelled RP- the O2/RP-1 engine. The maximum Iso for the l/A1, respectively. The Cstar efficiency for this RP-1 was 125.6 lbf-s/lbm and was loc_ited near propellant was 47% (at an O/F of 2.0) and low an O/F of 4.2. This maximum value is as 42% at a similar O/F. With Isp efficiency, the values ranged from 40% at an O/F of 2.0 different from the typically computed maximum near 2.7 for O2/RP-1 . The difference is due and the lowest value at that O/F is 36%. to the added nitrogen purge gas in the flow. The Cstar efficiency is plotted versus O/F in Heat Transfer Results Figure 9. With the O2/RP-1, the maximum Cstar efficiency was 69%. The Isp efficiency is The heat transfer results are presented shown in Figure 10 and, for the RP-1 in the Figures 20-22 in which the results for (ungelled), the maximum efficiency was 61%. RP-1 are compared with each gelled fuel type. These figures include the heat flux values RP-1/AI: 0-wt% A1. versus distance from the injector face for the four fuels. The highest heat flux occurs at In Figure 11, the Isp of the 0-wt% RP- cooling channel station 28, which was just l/Al engine is provided. The maximum Isp.for upstream the nozzle throat, 20.6 cm from the the 0 wt% RP-1/AI was 114.5 lbrs/lbm anit injector face. In each of the eases presented in was at an O/F of 2.6. Figure 12 illustrates the the heat flux analyses, the values were the representativecasesfor eachfuel type,andnot distance required to establish the combustion necessarily the highest heat flux or the highest zone, and also due in part to the deposition of Isp. For the. 55-wt% RP-I/AI, the highest Isp partially combusted gelled fuel at the injector case for th_s fuel was one of the lowest peak chamber interface. A combustion delay is heat fluxes for the 55-wt% fuel. The formation implied in the figure, with the heat flux near the of a metal oxide coating in the nozzle in the 55- injector being lower than the RP-1. Figure 21 wt% cases led to a reduction in the flux and this shows the reduction in heat flux for a set of reduction will be discussed in the succeeding runs for RP-1 and 0-wt% RP-1/A1. Q/A(1) sections. and Q/A(2) in the figure are the first two cooling circuits nearest the injectors face. It is During the calorimeter fLrings, the apparent that the overall flux for these two temperature of the cooling water did not always circuits in the 0-wt% RP-1/A1 cases (Runs 901- increase as expected. It was found later 958) are substantially lower than the through inspection of the test photos taken corresponding values for RP-1 (Runs 747- during some the firings with lower chamber 900). pressures that the rocket exhaust flow was separating from the nozzle. The heat transfer After the initial _w Q/A values, the flux beyond that separation point was minimal and increased to 2.3 MW/m, an increase due to the explains, in part, the fast drop in heat flux for combusting SiOz gellant, and then the flux the last two cooling channels in the heat dropped below the RP- lzheat flux value to a transfer analyses. Past testing also shows that low point of 1.0 MW/m. This drop in heat the nozzle heat flux w_ drop quickly after the flux implies that the chamber coating of peak nozzle heat flux. Flow separation did partially combusted fuel had formed and is not occur in all of the test runs, but it is noted cooling the latter part of the chamber. The peak as part of the explanation of the low nozzle heat nozzle heat flux was 3.9 MW/m. fluxes. 5 wt% RP-1/AI RP-1 Figure 22 depicts the RP-1 (Run 873) Figure 20 provides an RP-1 heat flux and 5-wt% RP-l/A1 (Run 986) heat flux profile (Run 873). The nozzle section near the profiles. As with the 0-wt% case, the heat flux throat had the highest I_egh flux. This result is has a profile where the flux is slightly lower typical of past testing.'" A stable than the baseline RP-1 value near the injector combustion zone established itself between the face, reached a peak in the chamber at 5 cm from the face, dropped below the RP-1 flux in 3 and 7 cm2region. After the heat flux reaches 1.7 MW/m, the flux is nearly constant until the last part of the chamber, and reached a final the flow enters _ae nozzle. The peak heat flux highest peak just before the nozzle throat. The was 3.6 MW/m and occurred at cooling peak flux in the nozzle was 6.5 MW/m. We channel station 28, 20.6 cm from the injector can infer that the coating of partially consumed face and just upstream of the nozzle throat. gel in the chamber reduced the heat flux in the The last two stations (see Table I0 show a very second half of the chamber. low flux because the flow became separated from the nozzle and therefore the flux drops off 55 wt% RP-I/A1 very quickly. Figure 23 shows the heat transfer 0 wt% RP- l/A1 profiles for RP-1 (Run 873) and the 55 wt% RP-1/A1 (Run 1019). The nozzle station 28 Figure 20 compares the RP-1 (Run near ,th_ throat had the highest heat flux (6.7 873) and 0-wt% RP-1/AI heat flux prof'des MW/m ), and this flux is the highest of all the (Run 908). The 0-wt% RP-1/A1 heat flux near cases. Higher heat fluxes were also observed the injector face is low, due to the time and in other 55-wt% cases. Figure 24 compares

10 thepeak nozzle heat flux for 12 different runs. fraction of nitrogen in the engine flow. The The Q/A variation is due to the thin metal oxide high nitrogen flow rate was used to protect the coating that formed on the nozzle surface, O2/H2 igniter in the center of the injector. Due insulating the nozzle wall from the combustion to several difficulties with flow rate gases. The values where the flux dropped and computations and measurements, these very then returned to a high peak are cases where the high nitrogen flows were used in the engine. oxide coating was removed after it had built up The nitrogen has two effects: reducing inter- on the nozzle surface. After runs 1013 and element mixing and lowering the combustion 1017, the build-up of the oxide was removed temperature, which may slow the vaporization with a small chisel. After run 1013, a large of the RP-1. The predicted chamber gas fraction of the coating could be removed and temperature for the O2/RP-1 case using the the heat flux returned to a high value on the high nitrogen mass flow was 2651 K (O/F = next run. It was clear that after run 1017, 0.44). Using O2/RP-1 with no nitrogen purge, though the coating was removed from the the chamber gas temperature was 3308 K throat and diverging section of the nozzle, (O/F= 2.6). This temperature drop may have a much of the coating remained on the significant effect upon the vaporization and converging section of the nozzle. This combustion efficiency of the RP- 1. The remaining coating caused the reduction in the nitrogen purge flow for the engine's igniter heat flux noted in Figure 24. was down the center of the chamber, with the 4 or 80-F-O elements surrounding the igniter. Metal agglomerations in the nozzle. The nitrogen could then tend to isolate some of When testing the 55-wt% RP-l/A1, metal the elements from one another. The RP-1 agglomerations occurred in the nozzle. This vaporization leng!_ was assessed using a code same effect occurred with the heat-sink engine. named ROCCID._ This code predicted a 72% We wished to avoid this buildup with the combustion efficiency for this 5.875-inch calorimeter testing and therefore cleaned the chamber with O2/RP-1. The short chamber nozzle surface and removed the A1203 as implies a lower vaporization level for the RP-1, quickly as possible after each run. An attempt and hence a reduced Cstar efficiency and was made to combat the agglomerations by performance. The short chamber was used f'n-ing the engine igniter to eradicate the small because of the availability of the calorimeter nozzle agglomerations as they formed. The chamber. Based on this analysis, the low agglomerations were reduced in magnitude performance could be increased by increasing over those formed with the heat sink nozzle. the chamber length. Instead of a thick coating that narrowed the nozzle throat, only a very thin coating of a few Another effect that may have lowered millimeters in thickness formed. This the engine performance is injector design. A agglomeration was a hardened metal buildup typical Oz/RP-1 injector operates at an O/F of that could not be easily removed. After taking 2.6 to 2.7. The O2/RP-1 injector was designed the nozzle off the test rig, the agglomeration to operate over a range of 3.4 to 4.2 O/F, so could be chipped off with a chisel and once that a wide range of testing could be conducted loosened, came off in large segments. During with a single injector. This design produced the previous heat sink engine testing, (after 15, an injector with an oxidizer post diameter of 2-second f'wings), the agglomeration had 0.144 inches and a fuel post diameter of reduced the throat diameter from 0.6 inches to 0.0225 inches. These larger O2 posts may 0.45 inches. have led to inefficient mixing of the RP- 1.

Analyses show that the heat transfer to the wall was significantly different for the RP- Some of the engine performance l/A! at 55-wt% versus the RP-1 fuel. Also, a numbers appear to be very low. These low gellant and an aluminum combustion delay was values are the result of the extremely high inferred in the 0% and 5-wt% RP-l/A1 cases

11 from the decrease in heat flux in the fh-st part of Once this thin layer was removed with a soft the chamber. A large decrease in heat flux in cloth, the metal surfaces exhibited minimal the last half of the chamber was caused by fuel erosion. An improved cooling technique might deposition in the chamber and nozzle. The be derived from this effect. After further engine combustion occurred well downstream analysis of the heat transfer data, a strategy of the injector face based on the heat flux might be formed to use this effect to improve estimates from the temperature measurements. engine lifetime. This location of the combustion zone and the deposition of partially combusted fuel on the With the ungelled RP-I and 55-wt% walls may have led to some of the reduction in RP-1/A1, there was no protective effect layer the expected performance. formed. There was discoloration and blackening of the O2/RP-1 injector faces and Observations injector-face erosion, pitting, and metal deposition that occurred with the 55-wt% RP- Heat Transfer and Potential Chamber l/A1. The greatest damage was done to the 55- wt% RP- l/A1 injectors after they had been used, removed, cleaned, and replaced in the The 0-wt% RP-1/A1 case showed the engine. Residual metal particles that had been potential insulation and cooling effect of the retained in the 02 manifold and the other deposition of partially combusted fuel on the injector flow passages were areas where 02 chamber walls. In Figure 25, the wall attacked the metal and, in some cases, caused temperatures for the RP-1 and 0-wt% cases axe severe injector damage. shown. In three of the last five temperature stations, the 0-wt% case has a lower wall Qther Gel Effects in the Chamber temperature than the RP-1 case. During inspection of the chamber during firings and Slumping of the gel in the chamber after after disassembly, a thin layer of partially a fixing did cause some unusual plume shapes combusted propellant coats the chamber and during the rocket experimental runs. Buildup nozzle, which is discussed in the next section. of a layer in the chamber occurred in the A similar coating of the engine had occurred converging section of the previous heat sink with the previous heat sink engine testing, rs'16 firings and also in the current calorimeter tests. An improved cooling technique might be There were longer times between firings with derived from this effect, but additional analyses the calorimeter due to the need to recharge the of the data are required. water cooling system and the time to estimate the uniformity of the temperature prof'de in the Self-protection of injectors chamber. These longer down times where the gel is allowed to flow down the chamber walls During the testing with gelled RP-1 and may have caused this slumping and buildup. the 5-wt% RP-l/A1, some residual propellant was found in the rocket chamber, coating the Propellant Drying in the Injector entire injector face and all of the chamber walls. This residual propellant was actually a mix of Using the igniter to clear the nozzle unburned fuel (with a gray or clear pink color) agglomerations also tended to evaporate the and some black or combustion products. liquid component of the gelled fuel during Figure 26 shows the typical shape of the fuel testing of the 55% RP-1/A1 with the deposits. This effect was perhaps due to the calorimeter. A relatively dry RP-1/A1 residue fuel lead of 0.2 to 0.3 seconds used in the would form in the fuel ports and the fuel dome. ignition sequence of the engine. After many This result is however confounded with the fact fu'ings, this added propellant did not that the injector had not been changed for three completely undergo combustion, and formed successive propellant types being tested: 0%, this smooth layer on all the internal surfaces. 5%, and 55% RP-1/A1. The injector was left in

12 placeovermultiplepropellantchangesbecause MW/m 2 for 0-wt% RP-1/Ai, 2.8,MW/m 2 for of thecomplexityof removingit. Although the 5-wt% case, and 3.6 MW/m" for the 55- the engine and injector were thoroughly flushed wt% fuel. After the initial high heat flux in the with Solvent 140 and nitrogen purges, some fast half of the chamber, the heat flux would buildup of gelled 0-w% RP-1 dry residue (pink drop rapidly in the second half of the chamber, gel only) was evident in the fuel dome once it droppir[g from their high values to about 1.0 was disassembled (5 to 10% by volume). This MW/m 2 for the 0- and 5-wt% cases, and 2.5 residue is partially attributed to the drying effect MW/m for the 55-wt% RP-1/Ai. Inspection of the igniter on the fuel in the injector. of the chamber after each ruing showed that fuel had deposited along the walls, causing the Firings with the 55% RP-l/Al resulted flux to drop. After leaving the chamber, heat transfer measurements with RP-1, 0-, 5-, and in repeatable performance, but the injector erosion was the greatest of any of the tested 55-wt% RP-l/Al gelled fuels showed that the fuels. Improving the cleaning process of the peak nozzle heat flux for some cases were 02 manifolds, or preventing the flow of double that of the RP-1 fuel combustion, particles into the manifolds would allow more especially with the 55-wt% RP-I/AI. cost effective and longer-lived testing of the 55- wt% RP-l/Al. More easily disassembled Concluding Remarks manifolds and injectors would allow better access to flow passages that would trap metal Though the high metal loading, 55-wt% particles. Prevention of the deposition of dried RP-1/AI, engine runs experienced some metal particles onto all engine surfaces will be agglomeration and erosion difficulties, the 0- very important for future high metal loading and 5-wt% tests ran well, with a Cstar metallized propellant testing programs, not to efficiency similar to the RP-1, and mention any operational propulsion systems. demonstrated a self-protective layer of gelled propellants and combustion products. The Conclusions most interesting results occurred with the 0% and 5% RP-1/A1 formulations. A thin layer of Rocket engine performance and heat gelled fuel and combustion products formed transfer were determined with a calorimeter throughout the chamber and protected the face combustion chamber and nozzle using RP-1 of the injector from virtually all burning, and metallized gelled RP-l/Al fuels. Rocket scoring, or other damage. combustion performance was not as expected, due to gelled fuel deposition in the combustion Many additional analyses can be chamber, a shorter than desired chamber conducted on the heat transfer characteristics of length, and a high nitrogen purge flow for the these engines. The time dependence of the engine's igniter. The combustion of metallized combustion and heat transfer has not been fully gelled propellants was realized with even investigated, the potential metal combustion lag simple 4- and 8-element triplet injectors. due to gelled and memllized gelled fuels has Rocket Cstar efficiency for the RP-1 fuel was only been analyzed in a preliminary manner, in the 65-69% range, while the gelled 0-wt% and much additional analysis of the data can RP-1 delivered 60 to 62% Cstar efficiency. provide many more insights. This work would The 5-wt% RP-1 exhibited a Cstar efficiency help improve the engine designs and eliminate range of 65 to 67% and the 55-wt% RP-1 fuel the losses due to fuel deposition. delivered a 42 to 47% Cstar efficiency. Though the performance obtained with The deposition of uncombusted fuel in the metallized gelled fuels is lower than that the chamber had a very strong influence on the required for beneficial applications to NASA heat flux profiles in the 0-, 5- and 55-wt% RP- missions, these results show the ways of improving future engine designs. Historical l/Al cases. The highest h_at flux in the chamber was 1.7 MW/m for the RP-1, 2.3 data with metallized gelled fuels has implied

13 that engines at higher thrust levels are able to 4) Allan, B. and Chew, W., "A Review of deliver the required high efficiency and Isp. Thixotropic Gels for Advanced Larger scale experiments will likely allow more Propulsion Systems," JANNAF realistic flow conditions, reduced influence of Propulsion Meeting, CPIA Publication igniter purges, and allow researchers to gather 602. Volume HI, November 1993. more engine data in a more-representative high- thrust rocket environment. 5) Arszman, J. and Chew, W., "rACAWS Propulsion Development These first rocket heat transfer Program," JANNAF Propulsion experiments with RP-UAI were a focus for Meeting, CPIA Publication 602. learning about and documenting the actual Volume HI, November 1993. rocket performance and any potential operational pitfalls. This work is an ongoing 6) Trikha, A., Warren, S., and Peters, J., set of analyses to determine the viability of "Advanced Crew Escape Capsule gelled propellants and their possible Technologies Program," SAFE applications to NASA missions. Continuing Association, Newhall, CA system studies will use the data from these and Proceedings, 1987, pp. 196-202. other experiments to find the appropriate uses of metallized gelled propellants. 7) Palaszewski, B. and Rapp, D., "Design Issues for Propulsion Systems Using Acknowledgements MetaUized Propellants," AIAA 91- 3484, September 1991. We'd like to thank NASA Headquarters, Office of Space Access and 8) Rapp, D. and Zurawski, R., Technology for their support of this work. "Characterization of RP- l/Aluminum Also, many thanks to Paul Molnar for his Gel Propellant Properties," AIAA 88- mechanical skills and the team of Bill Furfaro, 2821, July 1988. Ed Plum, Pablo Gutierrez, and Steve Culler for their electronics experience and assistance. 9) Mueller, D. and Turns, S., "Some Also, thanks to John Blankenship for his Aspects of Secondary Atomization of injector design work. Also, particular kudos to Aluminum/Hydrocarbon Slurry Diane Linne, Jack Reed, Gayle Roth, Jack Propellants," AIAA Journal of Swoboda, and Joe Zoeckler. Propulsion and Power, Volume 9, Number 3, May-June 1993. References 10) Wong, W., Starkovich, J., Adams, S., 1) Sanger, E., Raketenflugtechnio_ue, and Palaszewski, B., "Cryogenic Bedim R. Oldenberg, 1933, pp. 53. Gellant and Fuel Formulation for Metallized Gelled Propellants: 2) Wells, W., "Metallized Liquid Hydrocarbons and Hydrogen with Propellants," Space/, Aluminum," AIAA 94-3175, June Volume 45, June 1966, pp. 76-82. 1994.

3) Olson, T. and Setze, P., "Some 11) Palaszewski, B. and Powell, R., Combustion Problems of High Energy " Propulsion Using Fuels for Aircraft," NACA Preprint, Metallized Propellants," A/AA 91- 1958, International Symposium on 2050, June 1991. Combustion, pp. 883-893 and 7th International Symposium on 12) Palaszewski,B.,"Advanced Launch Combustion, London and Oxford, Aug Vehicle Upper StagesUsing Metallized 28-Sept. 3, 1958. Propellants,"NASA TP-3191,

14 on a Simulated presented at the JANNAF Propulsion Thrust Chamber Using H2-O2," NASA Meeting, Anaheim, CA, October 3-5, Technical Note, TN D-6638, February 1990. 1972. 13) Palaszewski, B., "Lunar Missions Schacht, R. and Quentmeyer, R., Using Advanced Chemical Propulsion: 20) "Coolant Side Heat Transfer Rates for a System Design Issues," NASA Technical Publication (TP) -3065, Hydrogen-Oxygen Rocket and a New AIAA 90-2341, July, 1990, also in Technique for Data Correlation," NASA Technical Note, TN D-7207, AIAA Journal of Spacecraft and March 1973. , May-June 1994. 21) Starkovich, J., Adams, S., and Palaszewski, B., "Nanoparticulate 14) Palaszewski, B., "Metallized Gellants for Metallized Gelled Liquid Propellants for the Human Exploration of Mars ," NASA TP-3062, Hydrogen with Aluminum," AIAA 96- November 1990. Also, AIAA Journal 3234, July 1996. of Propulsion and Power, Nov.-Dec. 1992. 22) Gordon, S., and McBride, B., "Computer Program for Calculation of 15) Palaszewski, B. and Zakany, J., Complex Chemical Equilibrium "Metallized Gelled Propellants: Oxygen Compositions, Rocket Performance, /RP- 1/Aluminum Rocket Combustion Incident and Reflected Shocks, and Experiments," AIAA 95-2435, Chapman-Joguet Detonations," NASA SP-273, Interim Revision, March presented at the 31st AIAA/ASME/SAE Joint Propulsion Conference, San 1976. Diego, CA, July 1995. 23) Muss, J., Nguyen, T., and Johnson, C., "User's Manual for Rocket 16) Palaszewski, B., "Metallized Gelled Combustor Interactive Design Propellant Experiences and Lessons Leamed: Oxygen/RP-1/Aluminum (ROCCID) and Analysis Computer Rocket Engine Testing," presented at Program," Volume I - User's Manual, the JANNAF/CPIA Gel Propulsion NASA Contractor Report 1087109, NASA Contract NAS3-25556, May Technology Symposium, Huntsville, 1991. AL, September 1995.

17) Linne, D., "Performance and Heat Transfer Characteristics of a Carbon Monoxide/Oxygen Rocket Engine," NASA Technical Memorandum 105897. February 1993.

18) Quentmeyer, R. and Roncace, E., "Hot Gas Side Heat Transfer Characteristics of a Subscale Plug Nozzle Rocket Calorimeter Chamber," NASA Technical Paper 3380, 1993.

19) Quentmeyer, R., Schacht, R., and Jones, W., "Hot Gas Side Heat Transfer with and without Film Cooling

15 Table I. Metallized Gelled Fuel Components: Weight Percentages

Metal Loading Components

RP-1 A1 SiO2 Suffactant frween 85)

0% 93.5 0.0 6.5 0.0

5% 90.0 5.0 5.0 0.0

55% 40.8 55.0 3.5 0.7

Table II Calorimeter Engine Geometry Data

n Axial Location from injector face (cm)

Combustion Chamber:

1 0.546 2 1.458 3 2.093 4 2.728 5 3.363 6 3.998 7 4.633 8 5.268 9 5.903 10 6.538 11 7.173 12 7.808 13 8.443 14 9.078 15 9.713 16 10.348 17 10.983 18 11.618 19 12.253 20 12.888 21 13.523 22 14.158

where: n is the axial station (starting at the injector face)

16 TableII (continued) CalorimeterEngineGeometryData

n Axial Location from injector face (era)

Nozzle:

23 16.027 24 16.939 25 17.851 26 18.763 27 19.675 28 20.587 29 20.978 30 21.951 31 22.939

where: n is the axial station (starting at the injector face)

Table Ill. Typical Metallized Gelled Propellant Engine Flow Rates and Performance: 55-wt% RP-1/A1, Run 1013

Fluid Mass How Rate (lbrn/s, kg/s)

02 0.0721 (0.0327 kg/s) RP-1/A1 0.0360 (0.0163 kg/s) N2 9_,269A_ f.0.1.l.El_k,g Total 0.3684 (0.1671 kg/s)

Other parameters for engine run 1013

Thrust (lbf, N), vacuum 29.34, (130.5) O/F 2.00 Chamber O/F 0.24 79.65 Isp, Obt'-s/]bm, Pc) Isv, vacuum Obf-s/lbm) 201.23 P_ (psi) 78.91 Cstar Efficiency 46.57 Isp Efficiency 39.58

17 200 PUMP-FED 02 /RP-1 /AI

180

v r. 160 ol p, m 140 m n- ..I 120 O SRB mmmm., 02 IRP-11Ah 55 wt% "-""-"""" 02 IRP-1 100 40 50 60 70 80

STS payload (1000 Ibm)

Figure 1. Liquid Rocket Booster Length vs. Payload Piston

Nitroge_

RP-1/Aluminum in Transfer I Piston/Cylinder

Tank _T _ RP-11N "_/ I Propellant _ _P- Flow to Piston-Cylinder Figure 2. Gelled Propellant Transfer Tank System Schematic

18 spo__ece

Injector _ _n__s_on chamber

ib _gniter_ [

RP-1 or[*"*-*] 4 o RP'I/AI I.._*** o2[ J

IM, P 6'141e4

Coolant channel inlet / outlet tubes (22 each for chamber, 9 each for nozzle)

Figure 3. Simplified Diagram of Engine Components and Configuration

55% wt% RP-11Ah Calorimeter

1.0

O ',= 0.8 t_ g:

= 0.6 x

,- 0.4 ,D [] E _] rail ra il m rm emma[] Im _" 0.2 0

m ra Q 0.0 > 0 1 2 3 4 5 0 Main Combustor Mixture Ratio (O/F)

Figure 4. Main Combustor O/F versus Overall Chamber O/F: 55-wt% RP-1/A1 with 02

19 • Theoretical Vacuum Isp A Test Data: Upper and Lower Bound

250

A

200

|

m V 150 4) (n m A A A Q. 100 E el cO mm ,'=_ 50 ¢.) 4) O. (/) 0 RP-1 0% 5% 55%

Propellant Type

Figure 5. Theoretical and Experimental Peak Isp for all Propellants

100

8O

(.1 z-- el 60 em

4) 40 L- m t_ 20

0 RP-1 0% 5% 55% Propellant type

Figure 6. Cstar Efficiency Range Summaries for all Propellants: At Peak Isp

2O 100

80

O 60

Qg O ii 40

Q.

m 20

0 I ! RP-1 0% 5% 55% Propellant type

Figure 7. Summary of Isp Efficiency Ranges for all Propellants: At Peak Isp

RP-I: Runs 747-900 200 O a.

.a 15o ¢R

J_

v 100

Q. E =_ o 50 =_

Q.

m 0 I T " " ! 0 1 2 3 4 5 Main Combustor O/F

Figure 8. Isp vs. O/F: RP-1 with 02

21 02 /RP-I: Runs 747-900 100

o 80 t-

ml o Rm 60

L. t_

O 2O

0 • • | 1 2 3 4 5 Main Combustor O/F

Figure 9. Cstar Efficiency vs. O/F: RP-1 with 02

RP-I: Runs 747-900

IO0

80

60

t_ 40 O

Q. 20 t_

0 | - _ o - , • • 0 i 2 3 4 5

Main Combustor O/F

Figure 10. Isp Efficiency vs. O/F: RP-1 with O2

22 0 wt% RP-1/Ah Runs 901-958

O 200 Q. g J2 m 160 (n | J: 120 4)

Q. [] [] E 8O n O [] gm qp_ (J 40 4) Q. O0

0 i . _ , . 0 1 2 3 4 5 Main Combustor O/F

Figure 11. Isp vs. O/F: 0-wt% RP-1/A1 with 02

0 wt% RP-1/Ah Runs 901-958 100

8O >,, O ¢.. 4) •_ 6 0 em

4) [] [] [] _ 40

in [] 0 2O

0 - | i - - i i 0 1 2 3 4 5 Main Combustor O/F Figure 12. Cstar Efficiency vs. O/F: 0-wt% RP-1/A1 with 02

23 0 Wt% RP-1/Ah 901-958 100

O ¢--

IB 80 O im ¢:

60 W m

O. E m [] [] ,i 40 O mm N-, lu [] O 20 O. 0rJ

0 1 2 3 4 5 Main Combustor O/F

Figure 13. Isp Efficiency vs. O/F: 0-wt% RP- ILM with 02

5 wt% RP-11Ah Runs 959-992 A O 200 n

160

| tO_ JQ m v 120 [] El [] m [] a. E 80 m_ O om Qu tO 40 Q.

0 0 1 2 3 4 Main Combustor O/F

Figure 14. Isp vs. O/F: 5-wt% RP-1/A1 with 02

24 5 wt% RP-1/AI: Runs 959-992

100

>" 80 e"

im 60 []

L-

40 0

2O

0 - . - _ | - . - | - 0 1 2 3 4 5

Main Combustor O/F Figure 15. Cstar Efficiency vs. O/F: 5-wt% RP-1/A1 with 02

5 wt% RP-11Ah Runs 959-992 100

== •8 80

60 m [] B_ ¢3. Ig E m •- 40

s_ o_ U _t 0. 20 03

0 - , - , • • 0 1 2 3 4 5 Main Combustor OIF

Figure 16. Isp Efficiency vs. O/F: 5-wt% RP-l/A1 with 02

25 55 wt% RP-11Ah Runs 993-1019

A O 100 E" J_ 80 m m

J_ m 60 [] Q m [] m rn El Q. 40 E =l O Im im 20 O

Q.

O ] • • • - • 0 1 2 3 4 5 Main Combustor O/F

Figure 17. Isp vs. O/F: 55-wt% RP-1/A1 with 02

55 wt% RP-1/AI: Runs 993-1019 100

80 0 r"

am 0 60 ¢:

t_ m 4O [] o [] []

20

0 0 1 2 3 4 5 Main Combustor O/F

Figure 18. Cstar Efficiency vs. O/F: 55-wt% RP-1/A1 with 02

26 55 wt% RP-1/Ah Runs 993-1019 IO0

>, o t- G) 80 em t_ _=em

G) 60 U) m Q. E 40 im i_rn o I_rn [] E! em q,. [] [] u 20 12. (/)

0 | , i , 0 1 2 3 4 5 Main Combustor O/F

Figure 19. Isp Efficiency vs. O/F: 55-wt% RP-1/AI with 02

Run 873 (RP-1) and 908 (0 wt%) 8

7 • RP-1 O RP-1/Ah 0 wt%

4 o

3 o o _: 2 0 0 Ii.OIiii O

1 o _o 0 0 5 10 15 20 25 Distance from Injector (cm)

Figure 20. Engine Heat Flux Data: RP-1 and 0-wt% RP-I/AI

27 RP-1 0-wt% RP-1/AI

2.0

A 1.5

• Q/A (1) O Q/A (2) 0 x 1.0 OO emm O ii O Q -r- 0.5 mm

!

0.0 7! ;0 800 850 900 950 Run number

Figure 21. RP-1 and 0-wt% RP-1/A1 Heat Flux Comparison: Channels 1 and 2, Nearest Injector

28 Runs 873 (RP-1) and 986 (5 wt%) 8

_7 • RP-1 04 O RP-11Ah 5 wt% O E 6

5 v x 4 m O _" 3 O t_ O G) O -r- O =mBQB • 2 umO _ • o • O _ 0 0 1 O 0

0 • • • m 0 5 10 15 20 25 Distancefrom injector(cm)

Figure 22. Engine Heat Flux Data: RP-1 and 5-wt% RP- l/A1

Runs 873 (RP-1) and 1019 (55 wt%) 8 • RP-1 7 A O RP-1/Ah 55 wt% O4 O E 6

5 v 0 o x 4 m 0 0 0 0 o R_ 3 t_ 0 0 0 O0 0 ill II -r- 2 0 mm mmm m 0 • • • 1 • • 0 • •

0 • , , 0 5 10 15 20 25

Distance from injector (cm)

Figure 23. Engine Heat Flux Data: RP-I and 55-wt% RP-1/A1

29 55 wt% RP-1/AI 8

A m Ol 7 E [] [] [] [] 6 [] [] V

X []

m 5 [] []

-r 4 []

• - i • • - = i CD CO 0 04 _!" (D GO 0 0 0 _-- ,r." ,r.- I- I- ¢_1 0 0 0 0 0 0 0 0

Run number

Figure 24. Engine Heat Transfer: Peak Nozzle Heat Flux Data for 55-wt% RP-1/A1 Calorimeter chamber only 400 • RP-1 0 RP-11Ah 0 wt% 380

q) t._ O *"m 360

E 340 _ _i _ 0 • • 0

m 320

0

3O0 ? 0 5 10 15 Distance from Injector (cm)

Figure 25. Temperature Profile for RP-1 and 0-wt% RP-1/A1

30 __ _zzle 1Igniter _njector

RP-1 or ( RP-1/AI

O2

S_pool piece --

or combustion chamber

Figure 26. MetaUized Gelled Propellant Engine Exaggerated Deposition Illustration

31 FormApproved REPORT DOCUMENTATION PAGE OMBNo. 0704-0188

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1. AGENCY USE ONLY (Leave blank) 2. REPORT DATE 3. REPORT TYPE AND DATES COVERED August 1996 TechnicalMemorandum 4. TITLE AND SUBTITLE 5. FUNDING NUMBERS

Metallized Gelled Propellants: Oxygen/RP-1/Aluminum Rocket Heat Transfer and Combustion Measurements

WU-252--50-01 6. AUTHOR(S)

Bryan Palaszewski and James S. Zakany

7. PERFORMINGORGANIZATIONNAME(S)ANDADDRESS(ES) 8. PERFORMING ORGANIZATION REPORT NUMBER National Aeronautics and Space Administration Lewis Research Center E-10400 Cleveland, Ohio 44135-3191

9. SPONSORING/MONITORING AGENCY NAME(S) AND ADDRESS(ES) 10. SPONSORING/MONITORING AGENCY REPORT NUMBER

National Aeronautics and Space Administration NASA TM- 107309 Washington, D.C. 20546-0001 AIAA-96-2622

11. SUPPLEMENTARYNOTES Prepared for the 32nd Joint Propulsion Conference cosponsored by AIAA, ASME, SAE and ASEE, Lake Buena Vista, Florida, July 1-3, 1996. Bryan Palaszewski, NASA Lewis Research Center, and James S. Zakany, NYMA, Inc., 2001 Aerospace Parkway, Brook Park, Ohio 44142 (work funded under NASA Contract NAS3-27186). Responsible person, Bryan Palaszewski, organization code 5310, (216) 977-7493.

12a. DISTRIBUTION/AVAILABILITY STATEMENT 12b. DISTRIBUTION CODE

Unclassified - Unlimited Subject Categories 20 and 28

This publication is available from the NASA Center forAeroSpace Information, (301) 621-0390. 13. ABSTRACT (Maximum 200 words)

A series of rocket engine heat transfer experiments using metaHized gelled liquid propellants was conducted. These experiments used a small 20- to 40-1bf thrust engine composed of a modular injector, igniter, chamber and nozzle. The fuels used were traditional liquid RP-1 and gelled RP-1 with 0-, 5-, and 55-wt% loadings of aluminum particles. Gaseous oxygen was used as the oxidizer. Three different injectors were used during the testing: one for the baseline O2/RP-1 tests and two for the gelled and metallized gelled fuel firings. Heat transfer measurements were made with a rocket engine calorimeter chamber and nozzle with a total of 31 cooling channels. Each channel used a water flow to carry heat away from the chamber and the attached thermocouples and flow meters allowed heat flux estimates at each of the 31 stations. The rocket engine Cstar efficiency for the RP-1 fuel was in the 65-69% range, while the gelled 0-wt% RP-1 and the 5-wt% RP-I exlu'bited a Cstar efficiency range of 60 to 62% and 65 to 67%, respectively. The 55-w_o RP-1 fuel delivered a 42-47% Cstar efficiency. Comparisons of the heat flux and temperature profiles of the RP-1 and the metallized gelled RP-1/A1 fuels show that the peak nozzle heat fluxes with the metallized gelled O2/RP-I/A1 propellants are substan- tially higher than the baseline O2/RP-I: up to double the flux for the 55-wt% RP-1/A1 over the RP-I fuel. Analyses showed that the heat transfer to the wall was significantly different for the RP-1/A1 at 55-wt% versus the RP-1 fueL Also, a gellant and m aluminum combustion delay was inferred in the 0% and 5-wt% RP-1/A1 cases firom the decrease in heat flux in the first part of the chamber. A large decrease in heat flux in the last half of the chamber was caused by fuel deposition in the chamber and nozzle. The engine combustion occurred well downstream of the injector face based on the heat flux estimates from the temperalure measurements.

14. SUBJECT TERMS 15. NUMBER OF PAGES 33 Gelled propellants; Metal propellants; Gellants; Rocket combustion; 16. PRICE CODE Metallized gelled propellants; Heat transfer A03

17. SECURITY CLASSIFICATION 118. SECURITY CLASSIFICATION 19. SECURITY CLASSIFICATION 20. LIMITATION OF ABSTRACT OF REPORT OF THIS PAGE OF ABSTRACT Unclassified Unclassified Unclassified

NSN 7540-01-280-5500 Standard Form 298 (Rev. 2-89) Presorlbed by ANSI Sld. 7.39-18 296-102

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