Reverse Osmosis As a Pretreatment of Ion Exchange Equipment at PSE

Reverse Osmosis As a Pretreatment of Ion Exchange Equipment at PSE

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Please Note: The author retains the copyright while the New Jersey Institute of Technology reserves the right to distribute this thesis or dissertation Printing note: If you do not wish to print this page, then select “Pages from: first page # to: last page #” on the print dialog screen The Van Houten library has removed some of the personal information and all signatures from the approval page and biographical sketches of theses and dissertations in order to protect the identity of NJIT graduates and faculty. ABSTRACT REVERSE OSMOSIS AS A PRETREATMENT FOR ION EXCHANGE AT PSE&G'S HUDSON GENERATING STATION by Steven Leon Public Service Electric and Gas Company's Hudson Generating Station has historically had problems providing sufficient high quality water for its two once through, supercritical design boilers. The station requires over 60 million gallons annually to compensate for system losses. The stations' ion exchange demineralizers proved to be costly to operate and overall inefficient in performance. Drawbacks include: short service cycles, periodic contamination of storage tanks due to premature breakthrough, prohibitively high chemical regenerant costs, excessive labor requirements, frequent resin replacement, and overall unreliable plant operations. A reverse osmosis unit was installed as a pretreatment to the demineralizers to offset these shortcomings. This did not eliminate the demineralizers, but vastly reduced the influent loading and extended the service cycle more than twenty fold. Significant cost savings have been realized, water quality was greatly improved, and plant reliability is secured into the next century. REVERSE OSMOSIS AS A PRETREATMENT FOR ION EXCHANGE EQUIPMENT AT PSE&G'S HUDSON GENERATING STATION by Steven Leon A Thesis Submitted to the Faculty of New Jersey Institute of Technology in Partial Fulfillment of the Requirements for the Degree of Master of Science in Environmental Engineering Department of Civil and Environmental Engineering October, 1995 APPROVAL PAGE REVERSE OSMOSIS AS A PRETREATMENT FOR ION EXCHANGE EQUIPMENT AT PSE&G'S HUDSON GENERATING STATION Steven Leon Dr: Hsin-Neng Hsieh, Thesis Advisor Date Professor of Civil and Environmental Engineering, NJIT Dr. Dorairaja Raghu, Member of the Committee Date Professor of Civil and Environmental Engineering, NET Dr. Su Ling Cheng, ember of the Committee Date Professor of Civil and Environmental Engineering, NJIT BIOGRAPHICAL SKETCH Author: Steven Leon Degree: Master of Science in Environmental Engineering Date: October, 1995 Undergraduate and Graduate Education • Master of Science in Environmental Engineering, New Jersey Institute of Technology, Newark, New Jersey, 1995 • Bachelor of Science in Environmental Engineering, New Jersey Institute of Technology, Newark, New Jersey, 1980 Major: Environmental Engineering Presentations and Publications: Leon, Steven, The Five Year Demineralization and Chemistry Plant Upgrade Plan Fossil Production Department, Public Service Electric and Gas Company, Newark, New Jersey, 1993. iv This thesis is dedicated to Ann and Dominick Leon. ACKNOWLEDGMENT The author wishes to express his sincere gratitude to his advisor, Dr. Hsin-Neng Hsieh, for his guidance and support throughout this research. Special thanks to Dr. Raghu and Dr. Cheng for serving as members of the committee. The author is especially grateful to Public Service Electric and Gas Company for their gracious cooperation in allowing the use of company data and information for this research, and for their foresight and latitude in their willingness to approve and implement cost-effective and innovative technologies. Special acknowledgment is extended to the personnel at Polymetrics Corporation, for their gracious cooperation. Special thanks to Marlene Bartek for her patience and tireless assistance with organizing and preparing this document. vi TABLE OF CONTENTS Chapter Page 1 INTRODUCTION 1 1.1 Plant Design 1 1.2 Water Quality Criteria 4 1.3 Demineralization Make-up Plant 6 1.4 Alternate Technology Investigations 9 2 REVERSE OSMOSIS SYSTEM DESIGN 14 2.1 Basic Concepts 14 2.2 Membrane Selection 16 2.3 Design Calculations 19 3 PRETREATMENT SYSTEMS 28 3.1 Pretreatment Overview 28 3.2 Membrane Fouling 29 3.3 Membrane Scaling 34 4 TEST METHODOLOGY 39 4.1 Test Methods 39 4.2 Continuous Monitoring 39 4.3 Grab Sample Testing 43 5 SYSTEM OVERVIEW AND CONTROL INSTRUMENTATION 48 5.1 System Overview 48 5.2 Plant Automation 50 vii TABLE OF CONTENTS (continued) Chapter Page 5.3 Monitoring Instrumentation 52 6 SYSTEMS PERFORMANCE 55 6.1 System Start-up 55 6.2 Demineralizer Water Quality 58 6.3 Demineralizer Throughput 61 6.4 Filter Performance 63 6.5 Permeate Quality 66 6.6 Performance Indicators 69 6.7 Reverse Osmosis Operations 72 6.8 Decarbonator Performance 80 7 COST ANALYSIS AND BENEFITS 81 7.1 Cost Analysis 81 7.2 Ancillary Benefits 86 8 CONCLUSIONS 89 8.1 Recommendations 89 8.2 Summary 90 APPENDIX A DESIGN CALCULATIONS 93 APPENDIX B SCALE CONTROL 98 APPENDIX C EXPERIMENTAL DATA 100 REFERENCES 107 viii LIST OF TABLES Table Page 1 Reverse Osmosis System Overview 27 2 Filter Media Description 31 3 Pretreatment System Components 38 4 Reverse Osmosis Alarm Set Points 54 5 Inspection Activity and Frequency 57 6 Demineralizer Influent Characteristics 60 7 Demineralizer Service Cycles 61 8 SDI Experimental Results 65 9 Water Quality Analysis 67 10 Cost Analysis 85 ix LIST OF FIGURES Figure Page 1 Hudson Generating Station Condensate and Feed Water Flow Path 2 2 The Demineralization Plant 6 3 Reverse Osmosis and Ion Exchange Economics 13 4 Osmosis and Reverse Osmosis Principles 15 5 Spiral Wound Membrane Configuration 18 6 Reverse Osmosis Element 24 7 Membrane Modules and Staging 26 8 Filter and Valve Arrangement 32 9 SDI Test Equipment 44 10 Reverse Osmosis Plant Flow Pattern 49 11 Reverse Osmosis Plant Control 53 12 Demineralizer Flow/Conductivity Relationship 58 13 Demineralizer Flow/Silica Relationship 59 14 Demineralizer Service Cycles 62 15 Influent/Effluent SDI Values 64 16 Reverse Osmosis Mass Balance 68 17 Recovery Rate 72 18 Normalized Product Flow 73 19 Individual Stage Pressure Differential 74 LIST OF FIGURES (continued) Figure Page 20 Rejection Rate 77 21 Permeate Silica Residual 78 22 Permeate Conductivity 79 xi CHAPTER 1 INTRODUCTION 1.1 Plant Design The Hudson Generating Station is the largest fossil fuel-fired electric generating station in PSE&G's system. The station is unique in that both of the steam units are once-through, supercritical design, meaning there are no drums in the boiler to collect and distribute steam, as are found in most generating units. The once-through design allows all the water in the boiler to steam simultaneously, prior to entering the turbine; the supercritical design involves the system pressure and temperature, which is in excess of 3500 psig and 1,050 degrees Fahrenheit. Supercritical, temperatures and pressures greater than 704 degrees Fahrenheit and of 3204 psig, denotes the point above which water can no longer exist in the liquid form regardless of applied pressure. The high amount of energy held in this steam makes these units much more efficient than the lower pressure units in the system. At these high temperatures and pressures the thermal expansion in the turbines, which drive the electric generators, is greatly enhanced, thereby, producing more work with less input. Unfortunately, the advantages gained from a supercritical design is a disadvantage from a water quality aspect, since the higher temperatures reduce mineral solubility making them more susceptible to precipitating on boiler tubes and turbine blades. The No.1 unit, built in 1964 and rated for 400 megawatts, is either gas or oil fired depending on the cost, and generates 2.8 million pounds per hour (MPH) or 5600 gallons 1 2 per minute (gpm) of steam. Unit No.2, built in 1968, is a coal-fired unit rated at 600 megawatts. This unit generates 4.0 MPH or 8000 gpm of steam. Figure 1 shows the flow pattern for the units. Each unit has an identical flow pattern. The condensate from the surface condensers is pumped by the primary condensate pumps at approximately 200 psig to the condensate polishers. These polishers contain mixed cation/anion resins that provide a water purity conductivity of less than 0.1 micromhos, or generally termed just micromhos. From here, the condensate is pumped by the secondary condensate pumps at approximately 800 psig through the low pressure heaters. The temperature at the outlet of these heaters is approximately 250 degrees Fahrenheit. Figure 1 Hudson Generating Station condensate and feed water flow path 3 The effluent of the heaters is pressurized in the main boiler feed pumps to approximately 4700 psig. The condensate is pumped through high pressure steam heaters into the economizer where the temperature increases to 420 degrees F. The flow continues into the boiler and exits the boiler as steam at approximately 750 degrees F. Steam is sent to the superheater section where it is dried and heated to approximately I 050 degrees F. At this point, the steam enters the Very High Pressure (VHP) section of the multi-stage turbine at a pressure of 3500 psig. The turbine spins at a constant speed of 3600 rpm.

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