5 [No. 160 ] G. W .R. MECHANICS’ INSTITUTE. SWINDON ENGINEERING SOCIETY. TRANSACTIONS, 1927-1928. ORDINARY MEETING.—DecemBER 1ST, 1927. Chairman—MR. K . J . C OOK. “LOCOMOTIVE BOILER WASHING” BY MR. W. H. PEARCE (MemBER ). Locomotive boiler washing is an essential factor in the attainm­ ent of economical locomotive operation. Hitherto it has not been commented on before this Society, and therefore a description of the development of present G.W. practice may be of value and probably some useful data will be forthcoming in subsequent discussion. Any changes in maintenance methods that will elimin­ ate trouble and tend to increase efficiency or reduce cost of repairs are always welcome subjects for discussion and investigation. Boiler construction has been improved by attention to details of design or method which have been found desirable, either for reducing the renewals required when under repair or for obtaining better results in service, and in this connection it is essential for observations under service conditions to be allied very closely with examinations when stripped down for repairs. The aim of the maintenance department is to keep all appli­ ances in as good a condition as possible, thereby securing a high percentage of the original efficiency. This needs special con­ sideration when dealing with the boiler, as it is the unit in which the heat is first transformed. It is thus important to keep the surfaces of all intervening plates between the heating agent and the water in the best condition for the transfer of heat. Com­ munication of heat is best when the surfaces are clean, both on the fireside and the waterside. The conductivity of metallic surfaces under different con­ ditions of scale deposits varies with the nature of the deposits. To describe in detail how such deposits may adversely affect 6 the earning capacity of a locomotive would involve a lengthy description of the ordinary routine work of engines and cannot be fully dealt with here. It may be pointed out, however, that a well designed boiler (in other words a G.W. boiler), when in its initial condition, is an efficient steam raiser.) In passing, it must be noted that water for boiler purposes is by no means always pure; it might, in fact, be looked upon as a weak solution of various kinds of matter, each item of which plays its own definite part when the water is heated in the boiler. No two waters are exactly the same and in addition, it must not be forgotten that, when being evaporated, the water is totally different from that originally fed into the boiler. A knowledge of these reactions and the methods utilised to deal with them is essential for the efficient handling of power plants. Waters which are naturally soft should always be regarded with suspicion, not be­ cause they are soft, but because the small amount of dissolved matter may have an acid reaction when being heated in the boilers. It is sometimes advisable to arrange for boilers operating with soft water to receive a supply of lime occasionally. In this way a thin scale will be maintained in the boiler and thereby protect the surfaces from corrosion. Hard water may be used with impunity, so far as corrosion is concerned, because the heating surfaces become covered with a protective coating of scale. During the process of steam raising, there is always a tendency for the impurities in the water to adhere to the surfaces that are transferring heat and to accumulate, even without any intermittent cooling process. The ever increasing deposit will more and more resist the passage of heat from these surfaces to the water, until the economic limit of heat transfer is reached. When boilers are forced, comparatively little scale or deposit may cause overheating of the firebox plates and tubes nearest to the firebox. In order to understand properly the subject of boiler washing it will be well to devote some little attention to the history of its development. Early methods were by means of cold water and were confined to making the best use of the maximum available head of washing water by using large bore leather hose pipes. With most shed hydrants the pressure would only give a horizontal jet of about 12’ from a 6” nozzle and deliver 20 gallons per minute, thus requiring over an hour to fill ordinary boilers. With such low pressures, the large leather pipes would often “ kink ” and pre­ vent a full flow. Large nozzles were used so that a good bulk of water was available, which was useful, but often it was without the necessary pressure, thus depriving it of the concentrated stream which is one of the essential factors in the removal of dirt from the water and steam exposed surfaces. The actual removal was, in the majority of cases, largely accomplished by various rods 7 suitably bent or twisted into scraper­like ends. These contrivances made it possible to dislodge some of the incrustations which could then be floated or drawn along with the water toward the outlet holes, until finally removed from the interior of the boilers. But it was often necessary to remove several tubes to allow of more effective cleaning work inside the boiler and to get at the fire­ box waterways. When these methods were in vogue the boilers were designed for comparatively low pressures, the number of hours in steam over any given period was small and they were worked by a smaller number of different drivers than under present day conditions. It was not unusual for drivers at that time to be responsible for their engine cleaning and boiler washing operations, and to the latter they gave special personal attention, reckoning it to be the fore­ runner of reliable and easy engine working throughout each week. The actual boiler washing was not entirely ineffective, but other changes were taking place and demanded something better than cleaning by means of cold water under normal pressures. The growing demand for increased engine working hours, with in­ creasing boiler pressures and capacities, also an all round speed­up of labour­saving devices to compensate for extra wages in de­ creased working hours, were a few ruling factors that led to the cleaning problem being made a subject for experimental consider­ ation by the G.W.R. In the foregoing remarks reference has been made only to cold water washing, but to associate cold water with hot boilers is obviously undesirable. All boilers being at a high temperature when under working conditions, any rapid cooling must be accom­ panied by contraction strains, whereas the boiler is designed for uniform internal pressures rather than unnecessarily quick cooling stresses. Liability to the latter must be avoided as far as possible. Nevertheless, until shortly before the introduction of superheater tubes (1906) it was the general practice to use cold water for washing out. A specified day was allotted to each particular boiler, with a view to ensuring that sufficient time should elapse between dropping the fire and releasing the pressure, in order to allow the temperature to fall by natural radiation to a recognised safe limit before application of cold water to the internal surfaces. If the off­duty time of the engine were limited, the pressure was reduced by using the injectors to fill the boiler to the top of the water gauge glass, thus providing the maximum bulk of hot water. The remaining pressure was released by opening the whistle valves, with whistles muffled, and by opening the steam heating or steam lance valves, or blower valve with smokebox door slightly open. With all steam blown out, the taper plugs were removed from the 8 top of the boiler and the hydrant nozzle inserted as near to the smokebox as possible. The blow­off cock was then opened sufficiently to allow the water to escape at the same rate as the cold water was entering the boiler, thus maintaining the water in the gauge glass at a constant level. This continued until the water issuing from the blow­off cock was cold. The water was then shut off and the boiler allowed to empty itself through the blow­off outlet, after which it was ready for washing out. It was very im­ portant that the cold water should enter slowly enough to ensure gradual cooling. If any error of judgment were made relative to the difference in temperature of the boiler interior and the washing out water, it would cause undue contraction and stresses in all parts. With such washing it was not unusual to hear of the breaking of firebox stays in the waterways. This alone would call for reflection with a view to introducing an improved system. When a locomotive fire is drawn and not immediately replaced by a new one, the heating surfaces are exposed to cold air currents and unequal contraction follows tending to cause leaks. The brick arch is composed of several cubic feet of firebricks which will retain their heat for a long period, and will not cool down at the same rate as the boiler surfaces exposed to the cooling down water. After blowing down, too much time was required for the washing process, thus taking up that which should have been available for any immediate repairs which were required. Not only was this system a source of delay and trouble in arranging sufficient off­duty hours, but other conditions existed which made it desirable to wash out mud or scale more effectively. The real difficulty, in districts that used hard water, was the removal of scale with the low pressure of the washing out water.
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